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Copter: SmartRTL causing Internal Error 100000 #22780
Comments
I am new here. Can i take this issue. |
@andrefreitas97 when it shows the error for the third time does it take time of 10 seconds or does it show the error immediately? |
Hello Shivam, I would recommend you start with good first issues. |
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@prathamesh7255 the error shows immediately after the third time I engage SmartRTL |
@andrefreitas97 I think the issue is almost resolved but as I was not able to reproduce the issue on my GCS, would it be fine for you to have an online meeting to clear some doubts? if it's fine, you can mail me the time which suits for you. you will find my email on my profile. |
@andrefreitas97, how many total waypoints were there when engaging smart RTL, three or more? |
There were none because it had just been turned on on my desk with no gps fix |
@rmackay9 sir, I think the absence of fixed GPS is causing the error.
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I think this issue is a duplicate of #17416 |
This PR could resolve the issue #17419 |
Bug report
Issue details
If I engage SmartRTL with a switch 3 consecutive times while the drone is disarmed I get Internal Error 100000 at the third time. I believe this should be some type of bug.
Version
4.3.3
Platform
[ ] All
[ ] AntennaTracker
[ X ] Copter
[ ] Plane
[ ] Rover
[ ] Submarine
Airframe type
Quad
Hardware type
Kakute H7
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